On December 3, 1990, two Northwest Airlines jetliners collided at Detroit Metropolitan Wayne County Airport.
Five seconds later (at 13:45 EST), the crew saw the Boeing 727, Northwest Flight 299 to Memphis, heading toward them on its takeoff roll.
[1]: 11 After the collision, the 727 flight crew immediately initiated a rejected takeoff and was able to stop the aircraft safely on the remaining runway.
Deciding that no immediate danger existed, he did not order an emergency evacuation, and the passengers and crew deplaned using the rear airstair after the aircraft was sprayed with fire retardant foam as a precaution.
[1]: 14 The accident was investigated by the National Transportation Safety Board, which determined the probable cause of the accident to be: a lack of proper crew coordination, including a virtual reversal of roles by the DC-9 pilots, which led to their failure to stop taxiing their airplane and alert the ground controller of their positional uncertainty promptly before and after intruding onto the active runway.
Contributing to the cause of the accident were (1) deficiencies in the air traffic control services provided by the Detroit tower, including failure of the ground controller to take timely action to alert the local controller to the possible runway incursion, inadequate visibility observations, failure to use progressive taxi instructions in low-visibility conditions, and issuance of inappropriate and confusing taxi instructions compounded by inadequate backup supervision for the level of experience of the staff on duty; (2) deficiencies in the surface markings, signage, and lighting at the airport and the failure of Federal Aviation Administration surveillance to detect or correct any of these deficiencies; and (3) failure of Northwest Airlines, Inc., to provide adequate cockpit resource management training to their line aircrews.
"[5] This article incorporates public domain material from websites or documents of the National Transportation Safety Board.